Completed job with signs of old bearing overheat. |
You can see here to the left, the photo shows overheating at the center of the alternator end plate. The brown color is burnt grease which has escaped the bearing. Actually the photo is the completed job before the sound case was put back . However, the "burnt" sign were still visible.
The first thing I did was remove the centre bearing support, on the alternator end plate.
Dry bearing |
I modified a puller to fit in the space available, to try to extract the bearing. In the end, so much force was applied, that a foot on one of the legs of the puller broke off. Soooo, time to remove the end plate and put a heavy bearing puller on it. You can see the sealed bearing has lost it's ability to hold it's own grease.
Trying to remove bearing without taking end plate off. |
Engine mount cut in half to facilitate removal. Assembly under way |
The end plate was removed, and I tried another very heavy duty bearing puller, to no avail.
Protection for windings etc against fine metal dust |
Now I was faced with cutting off the bearing with a Dremel. The end plate has a step on the inside surface which fits snugly into the generator casing. The end plate required several screw drivers, wedged in from the side, to get it started; and then I used a crow bar once a gap had been made, to pry it off. Be carefull not to damage either the end plate or generator casing. Use all your levers near the studs that remain on the generator casing, because that is the strongest area.
Bearing installed and generator case end cleaned and repaired |
Cut bearing. |
The outer shell of the bearing and the ball race were very easy to cut off. The inner race was placed next to a shoulder on the shaft, so I couldn't get the dremel saw all the way across. So, I turned it 90 degrees and cut down as far as I dared; starting near the shoulder and working back. It was tedious, but did a slightly better job than using a grinding stone.
One jacket end cleaned; nine to go. |
Now it was time to clean up the surface of both the end plate and alternator casing, for the new casket. However, I found Fischer Panda had epoxied the ends of the water jacket in the casing; placing first a thick gasket like cut out, inside the water jacket, and then the epoxy to the end of the water jacket.
I found one water jacket with nothing in it, but the remains of the epoxy. I proceeded to clean all the water jacket ends and release the epoxy "bungs".
Previous to this job, I had removed my sacrificial anode and found two of the gasket cutouts blocking the water hoses that are involved with the cooling. I wondered where they had come from, and Fischer Panda advised they were from the end plate gasket. Rubbish, The gasket was complete! Now I know. I've also found in the past, some of this epoxy in my heat exchanger. No wonder I've had over heating problems in the past.
Now in cleaning up this epoxy, I found a number of the cut outs had migrated into the water jacket. Lucky I have a special took for grabbing stuff in tight places.
To the left, some of the cutouts and epoxy removed. The smaller bits were not saved
Building up water jacket with J-B Weld |
I used J-B Weld to build up the "decayed areas", after ensuring the surface for the epoxy was clean and free of dust and "soft" aluminum.
J-B Weld takes about 4 hours to set and 24 to really harden. Selley's also has a similar product, but it sets in 3-5 minutes according to the directions. However, after trying it on another item, I found I only had about 1 minute of working time. I preferred the longer working time, although I often waited 20 minutes before applying J-B Weld to the surface.
The end of the casing, after the J-B Weld had hardened over night, was leveled with a dremel and fine burr, and checked with a straight edge.
Finally, after all surfaces were cleaned and checked for "Flatness", I used the supplied gasket and applied a thin layer of RTV high temperature gasket cement to both sides of the gasket. All studs were also given a coat of "antiseize" before the plate and nuts were applied. A gentle tap around the outer surface was required because of the shoulder that recesses into the casing. This can be seen in the inside of the gasket to the right.
The nuts were finger tighened, and the RTV allowed an hour to set up. Then final tightening done after the RTV cement had set up.
Engine mounts were applied and the capcitors and air intake module replaced. These were removed to facilitate the job and obtain exposure.
The small piece of generator casing cut out so that I could cut the engine mount in half was placed back with a small piece of aluminum plate, pop riveted to the fibreglass cutout, and screwed to the remaining sound proof case.
The engine and generator case were then filled with fresh water and antifreeze and bleed of all air. This took some time before the correct flow of water was to be had.
I feel that if I had of changed my generator casing to fresh water cooling sooner, that maybe this "corrosion" might not have happened. Regardless, while it was sea water cooled, the anode never deteriorated from it's new condition and feel FP's anode let me down. You can read about how I changed the water cooling here, so that both the generator casing and the engine, enjoyed fresh water only and heat exchanged through a heat exchanger.
Now it's a question of will this repair last a year until I can do a complete alternator casing changeout, and also, do we repair or install new? We have done four hours on the generator, and so far no problems.
Excellent Post! Came across this as I was rebuilding my gen head from an overheating problem. Thank you for sharing...
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