For most people traveling in "well to do cruising shores", usually have the means to obtain spares quickly. There are some areas though where spares are hard to get, or if freighted in, present customs difficulties; let alone the cost of it all. So, most cruisers carry what they think they will need. We thought we had most areas covered, but when we arrived in Fiji, we had three of our four heat exchangers go bad in less than one month. The transmission heat exchanger had small pin holes which leaked sea water. This was easily fixed with some solder. The main engine heat exchanger presented itself to my wife and I, by us noticing we were loosing engine fresh water from the "small top off tank". We suspected the fresh water was being lost through a hole inside the heat exchanger to the seawater side. Fortunately I had a spare main engine heat exchanger and replaced it out. The old one was sent for cleaning and testing and our suspicions were confirmed by the engineering firm. A small leak inside the heat exchanger.
(BTY, we hunted for a heat exchanger of any kind and could not find one in Fiji. We knew there would be some place that had one, but we felt we were chasing our "tails". So we went to plan "B". Get one where we know we can source one. Read below.)
The last heat exchanger was on the generator. A Fischer Panda (FP).
You will notice the round heat exchanger, under the motor and bottom hose. Just looking at it, I figured that it is going to be one hell of a job to get that out. We reversed flushed the heat exchanger, and got out a handful of particular matter. Inquiries, told us that this stuff actually "grows" inside and even though we fresh water flush the generator after each use, (flushing out the seawater from the heat exchanger) this wasn't enough to prevent stuff growing and blocking the tubes inside the heat exchanger. The flush worked for a while and the generator ran for some weeks, before it started to over heat again.
So, leaving the FP heat exchanger where it was, and removal for a time when we are in a better location, I decided to install another heat exchanger, out side the casing, and one which I could easily get to the hoses and heat exchanger itself. My wife was making a quick trip back to New Zealand, so I had her procure through contacts, a heat exchanger. This was modified with the appropriate hose tail size to fit the hoses used on the FP. I was very lucky to have someone help me with this while I sat in Fiji. Needless to say communication was a major factor in getting this done. Many thanks to Charles Webster.
When, the unit arrived, I set about modifing the cooling system for the new heat exchanger.
The parts, were carefully checked to make sure I had everything. The 19mm radiator hose is not shown in the picture but I had 4 metres of the hose.
The fresh water and raw water side of the FP heat exchanger were identified and the existing hoses removed from the fittings at the appropiate end. ( the other end was left attached to the FP heat exchanger, making for an easy reversal if needed.) New hoses were run to the outside of the FP casing, by which I had to drill 3 new holes in its base. The new heat exchanger was mounted to a cross member that sits behind the FP and in front of the main engine. The hoses were hooked up and the generator started. I'm pleased to report that the generator now runs for some hours and the water from the exhaust is no longer very hot but is warm to touch and the unit no longer shuts down itself due to over heating.
Some things to consider. I knew the FP heat exchanger was in poor location and if I ever get it out, will probably put removable end caps on it and mount it outside the sound proof casing just like the new one.
The new one works great, but in the next time the boat is laid up, I might also remove, (and now very easy to do so) and have it modified with removable end caps of a screw off nature.
I'll carry more heat exchangers as spares.
I'll carry a propane torch, easy flow rods, and silfos rods. Solder and soldering iron I already carry.
I will always consider the cost of an airfare to be part of my spares, to procure the item I neglected to have the foresight to carry.
As a bonus, the FP now shuts down from the control panel quickly, and I may remove the second solenoid modification, detailed in a prior blog, because it is not needed and the whole issue of not shutting down may have been due to a protective system in the control module. I'll give it another couple of months yet to see if all is well with the shut down. How do your heat exchangers look? Can you clean them easily? Happy cruising!
Various boat projects and ideas related to boating in general. Feel free to contribute your project. We are looking for the unusual; the new or different technique; or boat improvement project or product that others may find useful. Please email us at solaceadventures at gmail dot com to tell us about something you might have, to put on our blog site. Please, limit your comments to the subject or item(s) discussed. Businesses posting, that don't adhere to this, will be deleted.
Friday, July 22, 2011
Fuel Level Sender Units & Filling Cap
In cruising, you travel from country to counrty where environmental laws are increasingly becoming more strict. But we all want to look after the environment, right? Fuel spills are a serious mater and there are various ways to minimize these. Also, when under way, one sometimes has to top off the fuel tanks from Gerry jugs. This is made all the more harder if one has to do this on deck with rain or sea water washing over the deck.
(In one passage we carried 17, five gallon Gerry Jugs as well as our full 100 gallon tankage. We used all but 25 gallons in that passage in which we also endured a BIG storm. This system helped to do fuel transfer much easier, when being on deck was life threatening)
We installed, on each fuel tank, a filler cap, and while we were at it, installed a sender unit for fuel gauges. These were purchased through WEMA , a company that supplies sender units. As an aside, we also installed one of their special sender units on a holding tank; but have to report I'm less than happy with it due to it having to be cleaned periodically. A task I don't enjoy. But the Fuel sender units have been flawless and I can recommend them.
To cut the holes for the fittings, we used a regular hole saw found at most hardware stores, using some cutting fluid to help preserve the hole saw. I think we got about 5 holes cut before I had to purchase a new hole saw, which was cheaper than getting them plasma cut. Each item was sealed with an RTV automotive cement which formed the gasket and was impervious to diesel.
Now, I fuel the tanks from inside the boat to minimise the potential for a fuel spill into the ocean. The same applies with filling from gerry jugs. And of course, I have a very quick way now of checking how much fuel I have without the need to "dip" the tanks. A task which requires getting under the floor boards if done.
(In one passage we carried 17, five gallon Gerry Jugs as well as our full 100 gallon tankage. We used all but 25 gallons in that passage in which we also endured a BIG storm. This system helped to do fuel transfer much easier, when being on deck was life threatening)
We installed, on each fuel tank, a filler cap, and while we were at it, installed a sender unit for fuel gauges. These were purchased through WEMA , a company that supplies sender units. As an aside, we also installed one of their special sender units on a holding tank; but have to report I'm less than happy with it due to it having to be cleaned periodically. A task I don't enjoy. But the Fuel sender units have been flawless and I can recommend them.
To cut the holes for the fittings, we used a regular hole saw found at most hardware stores, using some cutting fluid to help preserve the hole saw. I think we got about 5 holes cut before I had to purchase a new hole saw, which was cheaper than getting them plasma cut. Each item was sealed with an RTV automotive cement which formed the gasket and was impervious to diesel.
Now, I fuel the tanks from inside the boat to minimise the potential for a fuel spill into the ocean. The same applies with filling from gerry jugs. And of course, I have a very quick way now of checking how much fuel I have without the need to "dip" the tanks. A task which requires getting under the floor boards if done.
Monday, July 18, 2011
Forestay Installation
When we purchased Solace it didn't have a forestay and yet we had running back stays. A pad eye was on the foredeck where perhaps a forestay should attach to, but that was just attached to the deck with no support from below such as a bulkhead. We decided we wanted a forestay, but with suitable support from below to take care of loads; as we intended to use it for a storm jib. Here's what we did.
The padeye was above our anchor locker which had no convenient bulkhead to attach to. So we created and glassed in a false bulkhead in a "V" shape to allow the anchor chain to continue to lay down. This was then finished off with a coat of "Flowcoat"; an air cure gelcoat.
Two rods were shackled to the new bulkhead. These had turnbuckles for adjustment of tension and PVC tube placed over for protection from the anchor chain.
Finally, the padeye on the deck was replaced with a folding padeye which matched the one seen here under the deck. Reinforcing between the padeye and underside of the deck was also undertaken. The two padeyes where then secured through the deck with countersunk bolts and nuts. The two rods where then shackled to the underside padeye to provide the support need for the forestay. We finished with installing our forestay and used a quick coupling cam lever to attached and remove the forestay from the padeye when not needed. Perhaps unluckily, one storm has proved it's effectiveness and I'm convinced our mast stands today because we had the forestay and running backs attached when a shroud broke.
The padeye was above our anchor locker which had no convenient bulkhead to attach to. So we created and glassed in a false bulkhead in a "V" shape to allow the anchor chain to continue to lay down. This was then finished off with a coat of "Flowcoat"; an air cure gelcoat.
Two rods were shackled to the new bulkhead. These had turnbuckles for adjustment of tension and PVC tube placed over for protection from the anchor chain.
Shackle to bulkhead |
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